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Re: Burnet Railfair



I observed that the maximum number of traditional sized cars seems to be about 50.  Pushing up to 59 caused problems starting the train and pulling cars off on the inside of the curves.  The slightly fewer cars did not seem to have this problem.  This will likely be a different number for Standard O since each car is heavier and might stay on better.  However, it could be a function of the load and the wheels.  
 
The crowds seemed quite heavy mid day both days, just to see the layouts.
 
We also had what may not have been a ground problem with the plug in the building.  We eventually found a grounded outlet and was able to connect with the clubs extension cords.  TMCC really needs a good ground to work correctly.
 
We had a bad hump at one of the switches into the yard on track 3.  We need to cut the carpet out from under this switch so it will sit on the board and line up better with the other tracks.  On a hard surface, the track and switch are the same height , but with the on carpet, the tracks sink down into it some and the switch does not.  This seems to be getting worse over time which would be expected as the tracks nestle down into the nap.  This should not take to long and would be a good thing to do at setup next time.  there is a knife in the tool box and the pattern is already on the board to cut around, the remove three screws and slide out the carpet and refasten the switch.
 
Buddy Burke (and wife) and Joe Maverick stopped by to see what we were doing and how things looked.  Also Tommy Shultz from Flatonia.  We handed out invitation to several promising people during the show.  hope some of them join us.
 
Scott
 
On Mon, 25 Aug 2003 17:12:06 -0500 "Steve Wise" <swise@aoot.com> writes:
 
Any volunteers to write a summary of the Burnet Railfair?
 
Ed
 
 
Perhaps everyone could submit their recollections on the event.  Then Ed could mush 'em all together into an article?  Just a thought...
 
 
I'll start off:
 
We had a good turnout for setup.  Thanks to all who came.  Ron, Adrian, Ira, Scott, Bob, Monk and I did setup.  Stevo was Fat Controller for setup.  We had a few kinks in the finished layout: 
 
we accidentally hooked the s-curve up wrong which caused the power for tracks 3 and 4 to be coupled!  We discover this friday night and fixed it.  It was fairly easy to seperate the S and reconnect it in the proper alignment.  The two remaining bugs were not discover until Saturday morning. 
 
I accidentally had a 2nd TMCC command base hooked to my sidings.  This cause dual TMCC signals to be put onto the rails.  The engines didn't like 'em much!  Simply turning off my unit solved this problem.
 
we had a short in a jones plug that caused the power for tracks 1 and 2 to cross.  We found this one by powering up track 1 and watching the voltage on track 2 (which was getting juice from track 1 due to the short),  and unplugging/replugging the jones plugs at each module until we saw the voltage fall on track 2.  Turns out there was a broken jones plug that had a loose track 2 wire that was touching the track 1 pin!!! Scott took this module home to fix it.
 
After these three bugs were worked out, the layout ran pretty good!!!  For future reference, both DCS and TMCC engines should be run on all tracks after setup to find these bugs.  Also, ensure that there are no voltage crossovers should be done too.  I blame the Fat Controller.   :-)
 
 
The crowd seemed to enjoy watching siding manuvers.  I certainly had fun doing them!   At one point, I had boxed my caboose in and needed help from one of the spectators on how to get it back out at the end of the train.  It was fun!  Adrian's transfer table worked great in both conventional and command mode.  Conventional is tricky, but once you understood what to do, it worked great.  One problem, though, is a conventional engine starts out in forward...than can be tricky! 
 
We had 2 wrecks which made for excitement:   ed accidently shot a coal car with his engine onto my siding module.  If it wasn't for some plexiglass adrian bolted to the end of the siding, ed would be out one coal car and an engine!  Scott had a runaway that cause a nice crash too.  I think both trains escaped without any injuries.  Perhaps we need a special page on our web site with "crashes of the tinplate trackers" pics???
 
The air conditioning, again, was marginal.  We should really push ASTA next year to ensure that there is adequate AC...
 
Teardown went smoothly, although everyone was hot and tired.  Ed, Rick, Ricky, Monk, Ryan, Adrian, Scott, and I all helped tear down. 
 
I think we made some good $$ on the Raffle.  Thanx to Lorraine for working the raffle table!